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back to 2078 index

2078 E50

TD124 Motor refurbish details

Disassembly:

DSC_5353.jpg (256195 bytes) The motor assembly after having been removed from the chassis with wiring harness intact.  There is no need to de-solder anything!

DSC_5354.jpg (162949 bytes)

DSC_5355.jpg (311232 bytes)

Measures and observations

DSC_5356.jpg (187204 bytes) The rotor shaft shows some evidence of having been in operation for approximately one half of a century.

DSC_5357.jpg (178426 bytes) The rotor shaft has been wiped down with a clean rag.  A micrometer reading of the shaft diameter was .1867 to .1865 inches.

DSC_5358.jpg (193915 bytes)

DSC_5359.jpg (244228 bytes) the thrust bearing ball is being held into the countersink at the shaft end by a bit of grease. 

DSC_5360.jpg (272646 bytes) and the grease is approximately one half of a century old.  It has hardened.  Turned to wax.

DSC_5361.jpg (270743 bytes) the disassembled pieces.  Note that the mounting shaft on the upper motor case has been removed and is now ready to accept MKII mounting shafts.

Clean-up.

Rotor and shaft: The rotor was thoroughly bathed and wiped down in acetone.  The shaft areas that were in bushing contact are now much less visible.  The rotor shaft diameter, after initial cleaning, measured .1867 to .1865, depending on the area being measured.  After a more thorough acetone bath, readings were .1865 uniformly from one end to the other with circularity (roundness) deviating less than .0001 inches.  My assessment is that there was a thin hardened layer of lubrication residue build-up and this has been removed.

The rest: The individual parts, casings, retainers, etc which will be reused have been cleaned/scrubbed in acetone to remove decades of accumulated grime. 

 

Assembly

New E50 motor bushings have been cnc machined out of Oilite Bronze to replace the original 50 year old bushings. The Oilite material is the same as the original.  Oilite bronze is a product name for a material also known as sintered bronze.  This particular type of bronze is highly porous, allowing lubrication to be retained within the bushing, providing a constant supply of lubrication to the rotating part.   The bronze is very soft and tends to wear far quicker than does the shaft which rotates within it. Two bushings from this new lot will go into this project motor.  

 

DSC_5362.jpg (229973 bytes) In the photo are the cleaned parts and some of the new replacement parts ready to go in.  New oil retaining felts.  New Oilite bushings (In the container of lubrication), will replace the old ones.  Note also the container of Loctite thread locker.  The thread locker will be used sparingly on the machine bolts and nuts to ensure that the bushing assembly does not vibrate loose.

DSC_5363.jpg (210035 bytes) A new bearing thrust pad has been cut.  The new pad material is Delrin infused with Teflon.  This Delrin/Teflon blend retains the sonic signature of plain Delrin but with a greater wear life.  Plastics have come a long way since 1957 when the TD124 was originally introduced to the world.

DSC_5364.jpg (217180 bytes) In this photo the lower motor case is partially assembled.  The lower cap with the thrust pad is beneath and being located by the two machine bolts. Visible are the new oil retaining felts after having been soaked in Texaco R&O 46 (turbine oil 20 wt).  The felts will feed lubrication into the porous bronze bushing over time to maintain a continuous supply of lubrication to the rotor shaft for another 50 years. In this shot the assembly awaits the placement of the  upper retaining cap  Fastener thread size is M2.5.

DSC_5369.jpg (200636 bytes) The cleaned rotor shaft and its new thrust bearing.

DSC_5370.jpg (166660 bytes) The original hardened steel ball bearing thrust has been replaced with this new silicon nitride ceramic bearing ball. Size is 2mm.  The new bearing ball features a surface which, unlike steel, completely lacks porosity.  Meaning improved surface smoothness.  Meaning less friction. 

DSC_5371.jpg (210642 bytes) With a dab of bearing grease, the new bearing ball is held within the countersink of the rotor shaft end.  Ready for assembly to the motor case.

DSC_5374.jpg (173119 bytes) The motor is assembled.  In this shot it can be seen that the original mounting shafts have been replaced/upgraded with the MKII length shafts.  It is to be fitted with a double grommet arrangement as per the TD124 mkII.  The sonic benefits of this upgrade is significant and should be carried out to all original TD124 (mk1) players.

Here's a side by side shot of the motor assembly before and after the upgrade/renewal.

E50b4after.jpg (105921 bytes)

DSC_5375.jpg (151100 bytes) preliminary bushing/shaft alignments. The motor bushings are of a self-aligning design.  It is necessary for the upper and lower bushing to share the same axis of alignment so that the rotor shaft may operate with the least amount of contact with bushing walls.

The adjust;  the upper and lower motor casings are gently moved (tapped) with a light/soft mallet into a position of relative alignment with each other. To gage the success or failure of each adjustment, the rotor is spun and observed for the amount of time it spins freely before slowing to a stop.  Longest spin time is desirable.  During this process, the case fasteners are only lightly snugged down in order to allow the upper and lower case shells to be easily shifted for position.  Once best alignment is achieved by this method, the 4 case fasteners are lightly tightened in an order that is least likely to alter the adjustments already made.  After tightening the rotor is spun again to check for free spin.

assemble the motor to the chassis and begin making bearing to shaft alignments for optimal motor operation.

After initial upper and lower bushing alignments, the motor was run steady, 24 hours/day, for one solid week.  Then the motor was observed for vibration as follows:

DSC_5412.jpg (127905 bytes) using a mechanic's stethoscope, the motor is listened to at various points on the outer motor body.  On the lower case, on the upper case, on the plates in the center. 

DSC_5410.jpg (119610 bytes) The 4 fasteners that hold the motor assembly together are loosened so that the upper and lower bushing cases can be manipulated for position again.  A small, light piece of hardwood is used to gently tap on the upper and lower motor casings in order to slightly adjust their positions relative to one another.  The stethoscope is the instrument that will allow us to know if the adjustment was good or not good by the noise level that results from the adjustment.

DSC_5413.jpg (127845 bytes)  When re-tightening the 4 fasteners it is observed that the adjustment is altered.  This I can tell by listening with the stethoscope. So then further adjustments are made to the upper and lower case position while the case is being tightened.  This is a painstaking process.  The reward for going to this trouble is a quieter running motor, and drive train that comes up to speed on the strobe within 1 minute of a cold start-up...and then holds a constant speed all day long.  A rock steady strobe observation.